still truckin…

Not a lot to report this week. Work was really busy and kept me from spending much time in the garage.

First up is my tires arrived! Nitto NT05 sizes 315/35-17 rear and 255/45-17 front. This should help me keep the Boss planted. Those rear tires are 12.5″ wide.

Started working on the heater. There’s a few things that bother me about it. Mostly that the halves mount through the firewall with simple self tapping screws threaded into plastic. Not the ticket to last a long time. So I made some strips to go inside the housing that I mounted rivnuts to. Used some high grade silicone adhesive and secured the strips in place. Now when I go to mount the heater, it will be much more secure.

The 6 slotted head screws will be button head stainless when installed. The 2 tek screws are just to help hold the strips in place while the adhesive sets.

Worked a bunch on the rear sheetmetal. Had to run the rear wiring harness and install a dropped trunk floor before I could start closing it up. The stock trunk floor is just flat. This adds a few cubic feet to be able to carry a bit more stuff. Also, over on the right, there was a small access panel to gt to the fuel line connections. Not very big, though. I cut it out and made a panel to cover it up. Nice and big access now.

All this aluminum takes time. Each piece has to be fitted, marked, removed, drilled, deburred, reinstalled then drill again into whatever it mounts to (another sheet or framework), removed, all the chips cleaned up, deburr again, then siliconed and riveted.

Installed the remainder of the trunk and rear aluminum. Once that was all done, finally got to install the rear bulkhead. What you’re looking at here is 12 pieces of aluminum, all siliconed and riveted together.

This about does it for the big aluminum pieces. I wont be working on the car this week due to some work commitments, but I’ll get at least 1 day in this coming weekend. Might start doing some electrical mods to the rear lights. Will do another update then!

brake system

Finished up the brake system, except for a few small details.

All lines are bent, secured and tight. Used the same Nicopp lines that are in the fuel system… no rust. Flares and hardware are standard 45* double flare. Time for reservoirs. Stock F5 has you using 1 reservoir to feed all the brakes. I want to do a little more for safety, so I am installing 2 reservoirs, 1 for front, 1 for rear. Then I’m doing a hydraulic clutch, so I need another for that. I like the F5 reservoirs, so got 2 more. I made a mount to hang these 3 reservoirs out of .04 aluminum and some 3/4″ angle.

Here it is test fitted and clecoed in place.

Engine compartment side

back side

Done

These are installed just in front of the drivers footbox in the engine compartment.

Just need to get some adapters and install the hoses, then the brake system is ready to be filled, leak checked and bled.

Fuel tank vent

This one is short n simple. The stock fuel tank vent is just a length of hose routed to be able to vent but not allow fuel to slosh out. The vent is needed to allow air to move in and out as fuel is added and used.

First, I upgraded the vent to a larger unit to prevent issues with how fast the fuel can be pumped in. Breeze big vent. Then I routed the hose up and over to the left side of the car and built this vent filter. It will help capture any fuel vapors to keep things smelling nice. Its filled with a filter bag and some filter charcoal that I bought at an aquarium store. Then one end has a 1/2″ hose barb fitting and the other end has a bunch of 1/4″ holes drilled in it. Its only temporary mounted… that will be finalized as the rear sheetmetal is installed.

Fuel system

Received some small parts that allowed me to finish up the fuel system. It is now complete from the pump inside the tank to the engine compartment. I’m using all 3/8 line, pressure and return, which will be plenty for the 427 (stock Fox 5.0 Mustang is 5/8 pressure, 1/4 return). The hard lines are nickel-copper (Nicopp) so they will never rust and are easy to form. All fittings are AN and the clamps are MS. Good aviation stuff. Nothing here is premade… I did all the bending, flaring, hose assembly and routing. System has been pressure tested to 125 psi (fuel system runs at 52psi) with no leaks.

The ends in the engine compartment are waiting until the engine is installed to build and install the final hoses.

Steering details

Issue with the steering: When all assembled, after everything is aligned, I need to be able to index the steering shaft to the steering rack to make the steering wheel straight when the car is going straight. The steering shaft fits so tight between the support bearing and the rack that its impossible to remove and index the splined adapter. I read several possible fixes on the F5 forum and ended up using a combination. First I moved the support bearing to the inside of the footbox. This gained about 1/8″ of room. However, it did require trimming the bearing retainer to fit.

This is the modified retainer compared to the original. Both must be trimmed.

The bearing now installed inside the footbox.

…and the view from the inside and why I had to trim it.

Still not enough to pull the splined adapter and re-index. However, another tip from the forum said it requires less space to pull the shaft from the adapter, so I pulled 2 set screws and voila!

End result is I can now remove 2 set screws, push the steering shaft up into the bearing out of the way and then remove and re-index the splined adapter.

Lots of work for something I’ll only have to do one time, but if I didnt do it, I’d most likely have to drive the car with an off-center steering wheel. And that would not make me happy.

Onward!

Comments / axle vent

Hi Friends!

First, my Blog Guru (brother) is looking into letting you guys post some comments. The problem is with spam and internet robots taking over. Might have to do a login which could be too much trouble for you. Still looking into it.

Lots done this week!

First, the axle vent. My Moser axle comes with a 1/4 NPT vent hole and a brass hose fitting. F5 has you simply running a hose up high and securing it so water doesnt get in.  Gotta be better, so I ordered this Ford axle vent that fits certain 86-14 Mustangs with the 8.8 axle. PN 4R3Z4022AA. Problem: the vent has a 7/16-20 thread, or a -4AN. So I also got this fitting from Earls, PN 916144. Install is easy-peesy and much better than a hose snaking all over the place.

Details, details…

Once again, it feels like I’m out there for hours and hours and not much gets done. Some of this work is slow going.. Also, while striving for perfection, my frustration levels rise when it doesn’t come out exactly right.

So I finally got the front & rear brake crossover lines done. The front one I did in the previous post had a wonky bend in it, and it bugged me to no end for several days. So I cut it off and remade the end with a line splice. Much nicer now. The rear line went very easily and is clamped to the underside of the triangle brace.

Working with the front brake lines, i bent and secured the line from the master cylinder to the front left brake. This is where the T is that splits the brake pressure off to both sides. Also installed the hoses for the brake and clutch reservoirs and got them clamped off. You can see the hard line in the top of this pic.

Also started bending up some of the 3/8 fuel lines. Got the pressure line from the filter to the engine compartment and ran the return from the engine compartment back to the end of the frame.

Of course, the ends in the engine compartment sticking up in the air are not final. I’ll get those cut to length after I get the engine and check clearances and access. These will be attached to stainless flex hoses going to the fuel injection.

So it seems like not much has been done, but I probably have something like 10 hours in bending and flaring brake and fuel lines, with still more to go. Slow, not very glamorous work, but it still has to be done.

Found out this weekend that it will take 3 weeks for Ford to build my engine after I order it, then maybe another week to deliver. I’ll be traveling for work extensively in April, so I’ll have to wait to order it. If you’re interested, here’s a teaser… Ford 427W

See yall later… and once again, thanks for following.

Devil’s in the Details…

Hi everyone!!

Been doing some things that aren’t very glamorous and take a good bit of time. Got my steering shaft installed…

…and spent about 4 hours installing a sound and heat barrier in the passenger footwell and floor. This will make the car have a more solid sound and protect the passengers feet from the exhaust headers, which will only about 8″ away.

Installed the flexible brake lines at all 4 wheels,

and today installed the brake line connecting the 2 front brakes.

Like I said, not a lot done but all these details take time.

I’m still a happy man…

Peek at the Gallery!

By the way, at the top of your screen on this page are 2 links, Home & Gallery. If you click on Gallery, it shows the thumbnails of all the pictures I’ve posted in order. Click on a picture and you’ll see it a bit larger. Click the crossed arrows and it goes full size. You may then scroll through with right and left arrows and see a lot more detail in the pictures.

See ya!

I got the aluminum back!

Finally! It took a month and I finally got my aluminum sheets back. All a nice grey with just a little bit of texture. Good stuff.

First thing I did was install the front suspension panels (also called ‘F’ panels) and built the passenger footbox. You’ll notice some of the panels are black… I painted these as once the body is on, these will not be seen.

Then I commenced to building the front suspension. I installed the upper control arms, Koni coil over shocks and the wheel bearing / spindles. I replaced the stock ball joints with hi performance parts from Howe Racing.

Then I built up the front 12.8″ Wilwood brakes. The calipers centered up very nicely.

Of course, this required a front wheel-to-brake interference check.

Is it looking like a car yet? Can ya start to see what I see?

By then it was getting cold and I dont have any heat in the garage. I’ll have to fix that by next winter. Put away the tools, cleaned up and put BOSS 427 to bed.

This is really starting to move now, considering I’m working on my own and still have to keep the job happy…

Thanks for visiting.

Few things have happened

I have fixed a small coolant leak at the heater select valve, and replaced the power steering pump with a unit that is setup and dyno’d for flow and pressure to match the Fox Mustang steering rack. Also has a reservoir mounted right to the side of the pump for excellent fluid supply.

威而鋼的副作用

我治療背痛已經有20年了,我見過許多因為服用高劑量威而鋼後出現肌肉酸痛需要到醫院接受治療的陽痿患者,各種年齡和不同嚴重程度。

  • 壯陽藥的選擇技巧

樂威壯的效果

即使兩次服用的劑量合起來不超過20mg的安全劑量,大部分陽痿患者每次服用 樂威壯都會想到服用10毫克效果夠不夠?需不需要增加到20毫克?吃最大劑量會不會損害人體健康?